Heating it & allowing it to cool too quick will have case hardened it making it difficult to drill or cut with a hacksaw etc. May need to soften it before you are able to cut it or drill it.
Hi Kenny, been there got that T-Shirt but different colour plough. Turned out the plough frame had a sleeve welded through it and the bolt was waisted and siezed in the sleeve and would never have come out through vari bracket hole.Yes, also looking at the picture I think the bolt is stuck because it has worn a lip into it where it pivots rather than seized with corrosion.
They're a nightmare, easing oil, a good drift and a big hammer, I eoiwo be tempted to keep giving it a sqhrt for 3 or 4 days before trying again. Might also be tempted to knock It back the other way. Ours is just welded solid now, got sick of the bloody things snapping.Overum. Bolt adjust vary width.
Just bought it but needs a few things sorted out.
Will get a pic later or tomorrow .
Pretty sure its a full depth bushIf you make a gig to locate the new bolt / bush, using a large enough drill can you drill out the bush with a mg drill? Hire shop will have them. Old weld will drill, slow and steady with coolant. You only have to drill the depth of the beam from both ends, that's if you have the room? New bush and bolt, run of weld, sorted. Well not as easy as that, but you get the idea.
Pretty sure its a full depth bush